Stock airbox reinstalled.

I took fifteen minutes this evening after it stopped raining to go out and put the stock airbox back into the car. The K&N Filtercharger with poorly-fitted air horn adapter and ghettotastic Home Depot sheet metal and weatherstripping “cold air box” came out and the car now has its torque restored down low and the hesitation between 3.5k and 4k RPM is now gone.

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